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Seismic retrofit of a truss bridge in Seto-Ohashi bridges

 Seismic retrofit of a truss bridge in Seto-Ohashi bridges
Author(s): , , ,
Presented at IABSE Congress: Resilient technologies for sustainable infrastructure, Christchurch, New Zealand, 3-5 February 2021, published in , pp. 125-132
DOI: 10.2749/christchurch.2021.0125
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This paper reports that isolation rubber bearings were newly installed instead of existing steel bearings as seismic retrofit in a truss portion of the Hitsuishijima viaduct in the Seto-Ohashi Brid...
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Bibliographic Details

Author(s): (Honshu-Shikoku Bridge Expressway Co. Ltd, (HSBE), Japan)
(Honshu-Shikoku Bridge Expressway Co. Ltd, (HSBE), Japan)
(Honshu-Shikoku Bridge Expressway Co. Ltd, (HSBE), Japan)
(Honshu-Shikoku Bridge Expressway Co. Ltd, (HSBE), Japan)
Medium: conference paper
Language(s): English
Conference: IABSE Congress: Resilient technologies for sustainable infrastructure, Christchurch, New Zealand, 3-5 February 2021
Published in:
Page(s): 125-132 Total no. of pages: 8
Page(s): 125-132
Total no. of pages: 8
DOI: 10.2749/christchurch.2021.0125
Abstract:

This paper reports that isolation rubber bearings were newly installed instead of existing steel bearings as seismic retrofit in a truss portion of the Hitsuishijima viaduct in the Seto-Ohashi Bridges, which is unprecedented method for highway-railway combined bridges in Japan. For the truss bridge, seismic performance evaluation was conducted and it was found that some members were damaged. In order to minimize retrofit work over the railway tracks, the isolation of truss girder was selected. For the truss girder isolation, the constraining effect of the long rail and the running safety of the train were studied. In the retrofit work, in order to minimize the impact on the expressway, railway tracks, and utility facilities, the structural change of the isolation rubber bearings and the displacement of truss girder caused by jacking up had to be studied. The support structure was adopted with a knock-off mechanism, and the effects of jacking up were confirmed by FEM analysis.

Keywords:
truss bridge seismic retrofit highway-railroad combined bridge isolation rubber bearing bearing replacement overall measures knock-off structure